Topic: Running better now ;)
Now that our VW is stopping well, it was time to work on making it go a little better. I had a performance intake that I was experimenting with, but the stocker got put back in so I could hunt down that elusive vacuum leak. My friend from the islands tipped me off to the throttle shaft seals on the 34 PICT, and that did the trick. I took 30 minutes and replace the intake manifold, but hooked everything back up to the factory air cleaner. With the stock cleaner, I did not have to rejet or adjust the carb. In this mode, the car ran smoother and quieter, and the powerband was wider and flatter. Freeway cruising was much easier, but I still did not have a lot of pickup when slowing back down and trying to get back up to speed again. It was better than before, but I could tell that there were restrictions in the intake system. Of course, I was also carrying 200 lbs of sound equipment and heading into a stiff headwind at 70mph, but it was not breathing all that it wanted to. The air inlet to the stock air cleaner is about the size of a thumb. Not enough for 1600cc at 5000rpm, and even more of a problem for a 1776cc which I suspect is actually in there. After I got back home (at a more relaxed pace), I installed a high flow air cleaner, modified the oil breather port on the new cleaner so it was not being forced against the generator, and adjusted the idle mixture out one full turn. Just for the record, the stock air cleaner on the Ghia has a weighted flow damper that puts a consistent restriction on the intake air. The valve is large and opens enough to not be the bottleneck in the system, but if you take it out, you run leaner at idle and part throttle. Putting an easier flowing filter also leans the mixture. Putting a less restrictive exhaust on also leans the mixture. You get the picture, and that's why I had to richen the idle and hand-adjust the main jet. Don't worry, I can go back to stock in 45 minutes, but the stock intake manifold has issues because it was designed for economy and ease of manufacture. It's still too lean and I need to step up the main jet size one notch, but now it's breathing much better and you can actually feel it accelerating in 3rd gear as opposed to merely gathering momentum.
1st and 2nd gear are a thrill, 3rd is nice for a change (no pun intended), and 4th not bad. I do have a 135 main jet that was tried, and power above 3000 rpm is crazy, but it was too rich. The stock is 127.5 I believe, and the modified jet equals about 129, but I think a 131 would be about right. The problem with air cooled engines is that you have to let them get cold before you pull the plugs to check mixture, so it takes a lot longer to get the mixture right the old fashioned way. A wideband AFR gauge would solve that...